Alright guys, some good news, some mishaps, and some strange (though potentially unrelated) results.
So this weekend I went downstairs to solve an issue I was having with the
carb puking everywhere. I got downstairs and realized I had forgotten to grab the Grizzly Float Valve I bought during the week. Had my girlfriend toss it down from the 6th floor to me on the street below. Gust of wind had other ideas. It blew back toward the building and landed on a ledge about 20ft up. Fuck.
Well, I can still remove the fuel pump right? I've heard of people removing it with no other modifications and being A-ok. Off I went, and god did it feel good to take all that crap off there. Here's a before after.
BEFORE:
AFTER:
I should also mention that the loss of the choke bracket seems like a smaller deal than it was made out to be. There are still wires running between the cylinders, both electrical and fuel, and a zip tie will keep all of these wires tidy and locate the choke right where it always was, as you see it in the photo above. I'll leave it like that until I relocate the ignition between the cylinders.
With the carb off (and cold) I used this time to route a fuel line from where the carb was previously puking, to the ground. I ran the crankcase breather line back to the left side of the bike, it snakes down between the clutch cover and pulley cover. Perfect.
Took her out for a ride and she ran great. Also the puking was gone! Both before AND after running. Also no issues starting it back up after a long ride.
At this point I'm satisfied and ready to head back inside and call it done. While walking back to the front door of our apartment complex though, what do I see there on the ground? Grizzly valve. It blew off the ledge and was back in my hand. Conscious kicked in and I decided I should probably put this in now or I never will. Waited for the bike to cool and installed the grizzly valve, being careful not to damage the carburetor's saddlebags.
A quick note, when looking at this photo you'll see two brass screws. One at float level on the right, the other below it and a bit more to the left. The one on the right holds the float on, the one below it holds the float needle valve body (grizzly valve in this case) in. Looking immediately to the right of that lower screw, you'll see one silver spec, the float, and then a black spec. That spec is the absence of space, as this grizzle valve has two flat sides which allow extra fuel into the chamber. During reassembly, be sure that the washer underneath the screw matches up with the float valve body, NOT the flat space as it will have nothing to hold down.
Additionally, the needle that comes with the grizzle valve body has a slight bend in it. I'm not sure which way it is supposed to face, or if it matters, but something to be aware of.
If you're going to do this, remove the bolts holding down the idle adjuster screw. If you remove that you'll be able to rotate the carb upside down. This would have been nearly impossible to do without being able to flip the carb, but maybe someone knows a better way than how I did it. I also used this time to ensure my
PMS screw was set correctly, I did 3 turns out.
Onto the strange portion of the results. I'm getting an usual stutter at 1/8 throttle. For example, if I'm cruising at 65 in 5th gear with the throttle off, the bike will stutter or bog down as I begin to open the throttle and then surge forward as I move beyond it. I'm inclined to believe this is a problem with either the PMS screw or the
pilot jet, but I can't be certain which. I pulled over to adjust the PMS during a 140 mile trip I took immediately after completing this mod, I turned it OUT another half turn (now at 3.5 turns out) to richen the mixture at that circuit as I felt the slowing was due to a lean condition and some popping I heard during highway riding. It didn't seem to make any difference and the problem persisted.
Is it possible that this is the result of my discolored coasting enricher? I'm planning to replace that as well but wasn't sure if it could also be causing this issue at the idle circuit. (PS: Ignore that black fuel line coming off the carb overflow section, this pic was taken before I rerouted it to the ground.)
Thanks for reading and for any ideas you guys have.