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Ernie Kennedy describes the rig and the blowout
preventer. ''It was so low to the ground, you
couldn't get anything for BOP's under it worth a
dime. It was an old thing...all it done was clamp
around the pipe....didn't have blind rams on it. For
a blind ram, what we had was an old Hughes 10 inch
gate valve. So, if we thought of it before it blew
in, we'd go down the cellar and close that old
valve. But nobody was gonna go in there and close
that valve afterwards - that was for damn sure! We
tried to close it on time, just for fun, while it
was on the ground - put pipe wrenches and snipes on,
and you couldn't turn it. It was all rusted to hell.
I think there was a little bleed-off line run out
there...just down to the end of the sump.
Fortunately, we never had to use that...very, very
fortunate."
Progress
was pitifully slow. The Lower Cretaceous gas sand
was water-bearing (so much for Weeks who had dreamt
about a hinge belt sand!). The D-2 equivalent was
not reached until April 27. From here on in there
was nothing but bad news. This was confirmed by the
four D-2 drill stem tests, only one of which yielded
20 feet of gassy oil with a small blow of gas. By
the time they had reached 5,212 feet, it was decided
to string eight lines instead of the six over the
crown block, thus improving the mechanical advantage
but increasing the time that it took to make trips.
Art Greene recalls the great compressional forces
the rig mast was now being subjected to, ''We all
knew what we could do." It was at this juncture,
decisions had to be made: Move the rig to drill a
direct offset to No. 1 or carry on until the rig's
capacity was reached. Did Calgary office realize
that the Franks No. 3 had already passed its limit?
Bit No. 39, a Hughes W7R got on bottom at 6:15
p.m., May 6. The author had returned from town,
ready for an uneventful night, little knowing he was
going to make history Johnny Morrow, the afternoon
driller, was hunkered down for a relaxed evening and
had got the cards out. lf all event well, even the
graveyard crew could sleep through to its long
change. But this was not to be. Suddenly at 5,374
feet, after having cut only 13 feet, drilling
speeded up to between three to five minutes to the
foot. Something was going on down below, but what
was it? The author allowed the drilling to continue
to 5,381 feet and shut the rig down, ordering
circulation for samples. Sample catcher Barker went
out to the shale shaker to watch for a change. The
combination of the small pump, the 3½inch drill
pipe, and the depth would mean that returns would
not reach the surface for hours. When they did, here
was this coarsely crystalline dolomite with not a
trace of oil staining in it. (This was the D-3,
later to be named Leduc. No chromatographs to detect
traces of hydrocarbons.) The roughnecks, ever
mindful of their need for easy tours, immediately
lashed out at the author when he was considering
pulling out for a drill stem test. All kinds of
threats and imprecations were hurled at him, but he
had been present at so many tests which flowed water
that another "dip in the ocean'' would not be out of
the ordinary.
When the graveyard crew came on shift, they were
also very riled up. Their whole night was to be
ruined because they had to pull out. The author had
gone in to get Bill Wedderburn, Dowell's tester.
Because of the late hour, and the feeling that it
was going to be water anyway, the author did not
contact Fred Killer, his boss, who was in charge of
all the well-sitters. This was a breach of routine
which would have far-reaching consequences the next
morning.
Clark Siferd, one of the sample catchers,
remembers he had agreed to work graveyard for Homer
Gingras. Siferd used to rack pipe routinely for
those chaps who wanted to get away for their 'long
change', but they never paid him! Bill Blinn was the
driller, Joe Henry was working derrick, and Clark
was racking pipe along with Art Greene. Wedderburn
made up the tool and they started back in at 3:00
am. The M.O. Johnson type was a full hole packer.
Giving all credit possible to the crew, they did not
run that packer (OD 6¼inch) too fast because there
was only 9/16 inch annular clearance in the 7-3/8
inch hole. What a hazard! It took them two hours and
forty minutes to get to bottom. At that time the
dart was dropped, actuating the valve at 5:50 a.m.
There was an immediate blow, increasing rapidly,
then declining while the pipe was loading itself,
but with what? Four minutes after the valve was
opened there was almost one MMcf per day gas
measured with the piton tube. Then all was
relatively quiet until suddenly, seven minutes
later, seven minutes since the dart was dropped, mud
and oil came to the surface. The effect was
astounding! A 200 foot high plume of fire shot up
into the air. Fortunately the flare line had been
secured. It had been sitting there in anticipation
of favourable results from the D-2 but had not been
needed - not until now. It didn't take anybody any
time at all to order the packer valve closed and
pull out of the hole.
Long before Lorne (Squeaky) Leeson, tool pushy
had phoned in his drilling report to Calgary at 9:00
a.m., the Toronto stock brokers knew. Wedderburn
thinks it was scouts watching both No. 2 and No. 3.
A contact in Vancouver is also believed to have
relayed word that Imperial had an oil well. Calgary
was still in the dark, being asked by 56 Church
Street (Imperial Oil's head office in Toronto),
"What is going on?" The era of REAL BIG OIL
in Alberta and Western Canada had begun that fateful
morning of May 7, 1947.
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