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At Atlantic No. 1, in lsd 13
Section 23, 278 ft. of surface casing were set, the
well having been spudded on October 2. The well was
then drilled without incident. The D-2 was diamond
cored and found to be non-porous, As was the habit
in those days, the well was completed in the D-3
"barefoot",18 It was put on production early in
November with an initial potential of 2,900 barrels
a day.
It is instructive to note what
Denton and Spencer said in their report on Atlantic
No.1 under the heading "Acknowledgements'':
Central Leduc Oils (Pyrcz lease)
made available a complete separator hook-up which
facilitated the completion of the well and saved
considerable expense while awaiting the fabrication
of a new unit (and Don Whitney came with it).
Leduc Consolidated (lessees of
the parcel offsetting to the east) made available a
casing head, string of tubing, tanks, line pipe
which could not otherwise be obtained, (This firm
later tried to sue Atlantic.)
Imperial Oil loaned their
swabbing equipment for the completion of the well.
Mr. Aubrey Kerr, Chief Geologist
for Imperial Oil, made available his experience and
advice regarding the value of the zones cored and
the proper position to locate the casing shoe. The
drilling contractor, General Petroleum Limited,
through their Superintendent, Mr. G.A. Wright, and
toolpusher W.Murray, performed all operations in a
workmanlike manner.
Mr. F. McMahon and Mr. B.
Lacey(!) were available at all times either in
person or by telephone for advice regarding
production equipment and procedures...19 There is
no mention of Lyle Caspell being involved.
Langston's "Conclusions and
Recommendations", (page 30 of the same report) point
up his care and concern for good engineering
practices. He elaborates on the flush production
which occurred on November 14, the well producing
about 120 barrels an hour with back pressure on the
tubing of about 300 psi and separator pressure 105
psi, He suggested that rates of flow should be
restricted to 150 barrels per day.
...Every effort should be made to
produce the well at the maximum rate in line with
good practice, bearing in mind that an error on the
low side would have no ill effect but that an error
on the high side might greatly decrease the value of
the property and lower the ultimate recovery during
its economic life.
Drilling operations then moved
over to No, 2 well site, a quarter of a mile east of
No. 1, in lsd 14 Section 23, It was spudded on
November 27 and only 279 ft. of surface pipe were
run. Trouble occurred by loss of circulation in the
D-3; it was successfully overcome, Langston recalls
that he warned Atlantic of the seriousness of this
but no special notice appears to have been taken,
The well was ultimately cased on December 29 and was
placed on production January 9, 1948 with about the
same potential as No. 1.
In this history, two or three
chroniclers stand out, One of them is Cal Bohme, a
native of Vermilion, now senior engineer with
Norwest, a Calgary based consulting firm, Earlier,
in the summer of 1944 at the age of 16, he had
toiled in the local dairy for $33 a month. His next
job was better: washing dishes in the Chinese cafe
because it paid $12.50 a week for only eight hours a
day. When Cal found out that roughnecking paid $6 a
day (a phenomenal amount of money!), he started at
Borradaile, near Vermilion, with G.P., on very heavy
oil. This area was booming because the crude, owned
by the CNR, could be burnt directly under the
boilers of their locomotives, thus reducing the need
for imported supplies.
...We would work on the service
rigs there, pulling tubing, bailing, and we'd be
covered with that black heavy tarry oil from head to
toe..,but at the end of the day they would give us a
wash cloth and a bucket of gasoline and you'd just
start washing yourself down from head to toe to get
that gooey old oil off.20
Cal's first exposure to a "wild
well'' was at Marwayne. "We encountered a tremendous
flow of water at fairly shallow depths and flooded
the rig out, pretty near upset it..."21 It was a
G.P. unit with a Hosmer; that tool turned out to be
of no use there. Cal arrived in Leduc in the fall of
1947 and started at Atlantic No.2. By now his G.P.
wages were $8 a day less $1.50 a day for board and
room in the company camp.
When the weather turned cold, it
was necessary to blow out, with natural gas, the
water lines which supplied the boilers, so there
would be no freezing in the lines. The water supply
came from Hector's system which had a sump over in
the north west corner of the lease, (later to be
taken over by oil). On one occasion, gas got into
the boiler house by mistake.
There was myself and Howard
Blanchard22 inside of one of three boilers that
provided steam for the rig and we were cleaning it
out with a water hose and scraper rods...can
remember the whole roof blowing off...and the
terrible concussion inside the boiler and. ..Howard
stuck his head out first and said, 'There's fire all
over. Let's get the hell out of here' and he went
out. The good thing about it, it was a very flimsy
structure. It just blew all the tin sides out of the
boiler house so we managed to get out of there
without any serious injury.23
Following the completion of No.
2, the next location was lsd 12 Section 23, the
south offset to No. 1, The Kerber brothers recall
having skidded the rig over during daylight hours,
thus cutting down on rig-up time. After No. 3, the
east offset to it, No. 4 was to be drilled, thus
providing four producers on the quarter section. But
fate now played a hand in the affairs of not only
General Petroleums, Denton and Spencer and Atlantic,
but also Imperial Oil, the Board and the Rebus
family: the mineral and surface owners of the
northwest quarter of Sectlon 23.
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